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Disclaimer: The Lessons Learned Database includes the incidents that were voluntarily submitted. The database is not a comprehensive source for all incidents that have occurred.
Because the bottle was located outside at the time of the event, and the hydrogen did not find a source of ignition while venting through the relief valve, nothing serious happened. The failed regulator was replaced and operations continued.…
For the use of mechanical fittings in hydrogen service, administrative controls should be in place, as in this case, to ensure that leak testing is conducted on a regular basis. It should never be assumed that every fitting is tight. Additional…
The following corrective actions have been taken:
Recommendation 1 - Overhaul and replace the diaphragms on all cells showing low-purity results. Check on a routine basis the individual cell purity levels to monitor the deterioration of performance of individual cells. Certain…
Hydrogen distribution lines should be designed and carefully inspected to ensure process equipment in the area is correctly and safely installed. Equipment subject to vibration should not be placed in contact with hydrogen lines or with other…
In this case, failure to recognize a run of tubing still maintaining pressure could have been avoided if such information was provided in a safety briefing. Knowledge of any job is the utmost importance in promoting and maintaining a safe working…
Installation
An important lesson to be derived from this incident is the need to carefully engineer and test all repairs and modifications to high-pressure process equipment.
This incident illustrates the danger of hydrogen being inadvertently released through blown water seals. Similar incidents have occurred in non-nuclear industrial facilities, but offgas systems present a special hazard because of the…
The lessons of this event fall into five categories: (1) proper in-plant communications during events, (2) proper valve application for use with hydrogen, (3) excess flow check valve set point, (4) heating and ventilation and air conditioning (…
These events show the importance of preventing combustible gas mixtures from accumulating in piping. In both of the above described events, hydrogen and oxygen gases apparently accumulated to a combustible level which then catastrophically failed…
The SS 24-inch pipe that failed was replaced with 1-1/4 Cr 1/2 Mo alloy pipe that is corrosion-resistant to SCC. A revised HTS bypass piping layout was installed to prevent the hazardous conditions that lead to the failure. A detailed hazard…
Based on the results of the company investigation and analysis of an amateur video, the company determined that the incident could have been caused by the failure of one of the following plant components:
· pipes leading to the reactor…
In addition to the probable causes listed above, the lack of a standard operating procedure for hydrogen leak detection was one of the probable causes of this incident. Additional contributing factors included the following:
- Severe pipe…
The following actions were proposed as a result of this incident:
Key:
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