Incident Synopsis
During development tests, a gaseous H2 test tank was over pressurized and ruptured. The tank dome was destroyed.

Cause
The pressure relief valves were set too high. In addition, the tank was not depressurized while being worked on. Safe distances, as required by the procedures for personnel safety, were not followed.

Incident Synopsis
While transferring liquid H2 from a tanker, the burst disk ruptured at 50 psi. The pressure limit for the operation was 30 psi.

Cause
The operator turned on the pressure valve and left it unattended, permitting pressure buildup past the allowed 30 psi.

Incident Synopsis
During a standard testing procedure, a 3,000 psig relief valve actuated at normal line pressure, releasing gaseous H2. The gaseous H2 combined with air, resulting in an explosion which damaged the test facility.

Cause
The relief valve was improperly set to open at line pressure, and the inspection was inadequate in that it didn't identify this error. Contributing cause was poor design of the venting system, which was installed in a horizontal position, causing inadequate venting and buildup of static electricity.

Incident Synopsis

A technician accidentally loosened critical bolts holding a fitting to the top of an H2 tank, which caused a large hydrogen leak in the dewar. The fitting contained various instruments, and upon loosening the third bolt, H2 gas exited through an opening in the seal. The Viton or neoprene O-ring was blown out of its groove and was immediately frozen, making it impossible to reseal the fitting cover. The area was evacuated, the dewar was vented and the gasket was replaced. The ullage space was not purged with helium gas during the gasket replacement, which may have been responsible for small leaks which developed during the transfer.

Cause

The fitting containing the instruments was mounted on a flange, which was in turn secured to another flange. view more

Incident Synopsis
A H2 delivery truck accident occurred on a highway. The truck was pulling a trailer containing gaseous H2. Upon entering a sharp curve, the truck and trailer started to weave and pushed to the side of the road. The truck and trailer rolled about 40 feet downhill; the trailer rolled over 1 1/2 times and the tractor once, ending in the upright position with the driver still in his seat. The truck was completely totaled, but little damage was incurred by the trailer. The trailer shell was satisfactory with normal venting through the stack. The rear cabinet doors were warped shut.

Cause

The accident occurred on a bad road, which was steep with many sharp curves. The driver was going too fast for the road conditions and the type of trailer being view more

Incident Synopsis
During transfer of liquid H2 from a commercial tank trailer to a receiving vessel, a leak developed in a bayonet fitting at the trailer/facility connection. The leak produced liquid H2 spray which enveloped the rear of the truck where the hand-operated shutoff valve was located. Emergency trained personnel, wearing protective clothing, except for proper shoes, entered the area and shut off the flow control valve. Reentry personnel suffered frost bite of their feet when shoes became frozen to the water-wetted rear deck of the truck.

Cause
A loose hose flange connection allowed leakage of cold fluid through the lubricated bayonet seal. This allowed cold fluid to contact and shrink the 'O' ring seal (made of Buna-N rubber), thus permitting view more

Incident Synopsis
While disconnecting a liquid H2 fill line from a liquid H2 trailer, liquid H2 escaped, burning a second man who was holding the hose. The man was burned on his hands and on his stomach.

Cause
The liquid H2 shut off valve was partially open, but both men assumed it was closed. Prescribed clothing was being worn.

Incident Synopsis
While a hot air dryer was being used to free a coupling in a hydrogen cryostat (an apparatus used to maintain constant low temperatures), a flash fire occurred. The H2 cryostat was being dismantled.

Causes
The temperature at the center of the cryostat was sufficiently low to liquefy air. The prescribed requirements for purging and bringing the cryostat to room temperature were circumvented. The H2 - air mixture was formed and ignition was assumed to be a spark from an open filament of the dryer.

Incident Synopsis
While attempting to replace a rupture disk in a liquid H2 vessel, H2 gas was released and ignited. In fighting the fire, liquid N2 was sprayed onto a second liquid H2 vessel located nearby. This resulted in cracking of the outer mild steel vacuum jacket. The loss of the vacuum caused a rapid increase in pressure and rupture of the burst disk of the second vessel. H2 boiled off and was burned in the fire.

Cause
The rupture disk was being replaced with a load of liquid H2 in the vessel and no separating inerting gas. The H2-air mixture was probably ignited by static discharges. Rupture of the second vessel burst disk was caused by the low-temperature exposure of the mild steel vacuum jacket.

Incident Synopsis
During pressure testing of a H2 tank for investigation of quick-release manhole cover, the tank burst at a pressure between 60-67 psig. Flow regulators indicated peak pressure of 67 psig.

Cause
The tank was over pressurized. A mistake was made in interpreting the blueprint, believing the tank was designed to withstand 150 psig, yet the actual design limit was 50.7 psig.