A distillate dewaxing unit at an oil refinery was undergoing hot hydrogen regeneration of the catalyst when an explosion occurred. Catalyst regeneration is a periodically performed procedure, in which the normal liquid hydrocarbon feed is stopped and a hydrogen-rich gas mixture is fed through the catalyst bed for which the normal operating temperature is raised from 700F to 800F. During the catalyst regeneration process the reactor pressure is increased from normal operating levels just below 600 psig to about 640 psig. A pipe failure occurred as a sudden and complete rupture of the 10-inch diameter line at the exit of one of the two reactors. Security video revealed that the release rapidly exapnded and the hot gas mixture ignited shortly after rupture. A shock wave from the resulting view more

A previously identified generator hydrogen gas leakage into the stator cooling water system exceeded the predetermined maximum operational allowance and the nuclear plant was shut down from 100 percent power in accordance with plant operating procedures. The leak was identified by monitoring the stator water cooling system detraining tank. Following reactor shut down and generator rotor removal, a small hole was located in the collector end winding area of a slot on the top stator bar. A small particle of carbon steel (estimated to be 2 mm/0.078 inch by 0.6 mm/0.023 inch) is believed to have caused the damage. The source of the carbon steel particle was either foreign material introduced during previous generator internal work or from a phenomenon called "back-of-core burning view more