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CHECK OUT OUR MOST RELEVANT INCIDENT LISTINGS!

Disclaimer: The Lessons Learned Database includes the incidents that were voluntarily submitted. The database is not a comprehensive source for all incidents that have occurred.

Immediate Corrective Actions

  1. Fuel cell test stand was shutdown and sent to manufacturer for investigation.
  2. Carbon dioxide fire extinguisher installed in laboratory.
  3. Formal process hazard review performed…

In addition to resealing the glove box window, a positive pressure of argon gas was maintained inside the glove box while the course of action was planned. Subsequently, the glove box was cleaned up by specialized hazardous materials personnel…

  • All tank trailers should have a safely accessible auxiliary shut off valve in case of spills.
  • Emergency personnel need to have access to all of the appropriate protective clothing, including shoes. Liquid hydrogen is stored at 20…

Normally hydrogen fires are not extinguished until the supply of hydrogen has been shut off due to the danger of re-ignition and explosion. During a gas leak/fire, it is important to shut off the source of the hydrogen if it is safe to do so. If…

Lessons Learned The site initiated the establishment of a field patrol and strengthened their onsite monitoring of mechanical equipment during a plant-wide temperature rise.

  • Quantitative control of tightening torque on bolts…
  1. The dilution water for making a polythionic acid aqueous solution was changed from industrial water to pure water to lower the chlorine concentration in the piping.
  2. Water that accumulated in the drain was removed before heating…
  • Operation and management of the hydrodesulfurization unit should be strengthened to account for abnormal phenomena such as local corrosion.
  • The safety review system for remodeling existing equipment and facilities should be…
  • Verify that all PRDs contain fuse-backed adapters.
  • Explore elimination of rupture disk PRDs and substitution of spring-style relief valves.
  • Develop new hydrogen unloading procedure using a written checklist. * Add…

Failure of a diaphragm is not infrequent, but the seizure of the main nut threads is very rare. The manufacturer claimed this had never occurred before with this type of unit. The broken plunger is likely the result of poor instructions/…

The visiting intern had several years of experience in research projects and tasks that were similar to those in progress at this laboratory. This led to the incorrect assumption that formal introductory training for this laboratory was…

After the aforementioned incident, a rigid cage was designed to protect the reactor from external conditions, and to protect the contents of the hood and any experimenter from the reactor, in the event of a pressure burst from the reactor cell.…

High-pressure fueling hoses should be examined daily for signs of external damage, including corrosion, abrasion, cuts, and kinking. High-use fueling hoses should be replaced every six months.

  1. Revise fire protection operations surveillance tests to include a maximum of 110% of the agent net weight to prevent over-filled cylinders from being placed in service.
  2. Identify cylinders currently in service that exceed the 110…
  1. Consider periodic testing of breakaway device.
  2. Consider determining shear force limit of vehicle receptacle adapter fittings.

Mounting hardware incorporated polymeric braces not suitable for long-term exposure to sunlight and temperature extremes. With time, the polymeric materials had disintegrated, allowing the mounting brackets to become loose. In addition, the…

The SS 24-inch pipe that failed was replaced with 1-1/4 Cr 1/2 Mo alloy pipe that is corrosion-resistant to SCC. A revised HTS bypass piping layout was installed to prevent the hazardous conditions that lead to the failure. A detailed hazard…

  1. Place signs on all liquid hydrogen tanks indicating that no water is to be put on the vent stack.
  2. An additional secondary backup vent stack was added to liquid hydrogen tanks. This secondary stack is designed to be used only if…

The turbine components that caused the vibrations were a retrofit design which had been in service for about two years and were under warranty from the vendor. The root cause analysis of the event determined that the damage was caused by a defect…

The direct cause of the over-pressurization of the two drums was the repackaging of the phosphoric acid into metal UN1A1 drums and the resultant hydrogen gas generation within the sealed drums. At the time of this incident (1997), 49 CFR and…

The investigation team concluded that hydrogen gas was released through a failed 19-inch diameter gasket and ignited under the roof of the compressor shed where it was partially confined. Some gas escaped from the shed prior to the explosion, but…

Key:

  • = No Ignition
  • = Explosion
  • = Fire
Hydrogen Incident Summaries by Equipment and Primary Cause/Issue
Equipment / CauseEquipment Design or SelectionComponent FailureOperational ErrorInstallation or MaintenanceInadequate Gas or Flame DetectionEmergency Shutdown ResponseOther or Unknown
Hydrogen Gas Metal Cylinder or Regulator 3/31/2012
4/30/1995
2/6/2013
4/26/201012/31/1969  3/17/1999
11/1/2001
12/23/2003
Piping/Valves4/4/2002
2/2/2008
5/11/1999
4/20/1987
11/4/1997
12/31/1969
8/19/1986
7/27/1991
12/19/2004
2/6/2008
10/3/2008
4/5/2006
5/1/2007
9/19/2007
10/31/1980
2/7/20091/24/1999
2/24/2006
6/8/1998
12/31/1969
2/7/2009
9/1/1992
10/31/1980
10/3/2008 
Tubing/Fittings/Hose 9/23/1999
8/2/2004
8/6/2008
9/19/2007
1/1/19829/30/2004
10/7/2005
 10/7/2005 
Compressor 10/5/2009
6/10/2007
8/21/2008
1/15/2019
  10/5/20098/21/2008 
Liquid Hydrogen Tank or Delivery Truck4/27/198912/19/2004
1/19/2009
8/6/200412/31/1969 1/1/197412/17/2004
Pressure Relief Device7/25/2013
5/4/2012
1/15/2002
1/08/2007
12/31/1969    
Instrument1/15/20193/17/1999
12/31/1969
2/6/2013
  11/13/73  
Hydrogen Generation Equipment7/27/1999  10/23/2001   
Vehicle or Lift Truck 7/21/2011    2/8/2011
12/9/2010
Fuel Dispenser 8/2/2004
5/1/2007
6/11/2007
9/19/2007
 2/24/2006
1/22/2009
   
Fuel Cell Stack      5/3/2004
12/9/2010
2/8/2011
Hydrogen Cooled Generator   12/31/1969
2/7/2009
   
Other (floor drain, lab
anaerobic chamber,
heated glassware,
test chamber,
gaseous hydrogen
composite cylinder,
delivery truck)
 11/14/1994
7/21/2011
7/27/1999
6/28/2010
8/21/2008
12/31/1969
3/22/2018
  6/10/2019
  • = No Ignition
  • = Explosion
  • = Fire
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