What is Lessons Learned?

What is H2LL?

This database is supported by the U.S. Department of Energy. The safety event records have been contributed by a variety of global sources, including industrial, government and academic facilities.

H2LL is a database-driven website intended to facilitate the sharing of lessons learned and other relevant information gained from actual experiences using and working with hydrogen. The database also serves as a voluntary reporting tool for capturing records of events involving either hydrogen or hydrogen-related technologies.

The focus of the database is on characterization of hydrogen-related incidents and near-misses, and ensuing lessons learned from those events. All identifying information, including names of companies or organizations, locations, and the like, is removed to ensure confidentiality and to encourage the unconstrained future reporting of events as they occur.

The intended audience for this website is anyone who is involved in any aspect of hydrogen use. The existing safety event records are mainly focused on laboratory settings that offer valuable insights into the safe use of hydrogen in energy applications and R&D. It is hoped that users will come to this website both to learn valuable lessons from the experiences of others as well as to share information from their own experiences. Improved safety awareness benefits all.

Development of the database has been primarily supported by the U.S. Department of Energy. While every effort is made to verify the accuracy of information contained herein, no guarantee is expressed or implied with respect to the completeness, causal attribution, or suggested remedial measures for avoiding future events of a similar nature. The contents of this database are presented for informational purposes only. Design of any energy system should always be developed in close consultation with safety experts familiar with the particulars of the specific application.

We encourage you to browse through the safety event records on the website and send us your comments and suggestions. We will continue to add new records as they become available.

How does H2LL work?

If you have an incident you would like to include in the H2LL database, please click the "Submit an Incident" button at the top of the page. You will be asked for a wide range of information on your incident. Please enter as much of the information as possible. In order to protect your and your employer's identities, information that may distinguish an incident (your contact information, your company's name, the location of the incident, etc.) will not be displayed in the incident reports on H2LL.

Lessons Learned Corner

Visit the Lessons Learned Corner Archives.

Key themes from the H2Incidents database will be presented in the Lessons Learned Corner. Safety event records will be highlighted to illustrate the relevant lessons learned. Please let us know what you think and what themes you would like to see highlighted in this safety knowledge corner. You can find all the previous topics in the archives.

A process area alarm activated. The alarm was caused by an instrument channel located above a reaction vessel off-gas system final HEPA filter canister, which indicated 25% of the lower explosive limit (LEL) for hydrogen. Since the only source of hydrogen is from the reaction vessel during the reaction of sodium with concentrated sodium hydroxide, the immediate actions were to shutdown the reaction process and place the facility in a safe condition.

The root cause was inadequate or defective design. Had the pre-filter drains been vented to outside the building, no hydrogen could accumulate in the process area. The corrective action for this is to complete an Engineering Task Authorization (ETA) to install a sample/drain collection system with loop seals to prevent any release of view more

A deficiency was discovered in the application of a hydrogen sensor in the Rotary Mode Core Sampling (RMCS) portable exhauster. The sensor is installed in the flow stream of the exhauster designed to be used with a RMCS truck for core sampling of watch list tanks, and is part of the flammable gas detector system. During the previous week, a quarterly calibration of the sensor, per maintenance procedure, was attempted by Characterization Project Operations (CPO) technicians. Ambient temperatures during the sensor calibration were approximately 20 to 30 degrees F. Inconsistencies in calibration results and the failure of the sensor to meet the response-time calibration requirement lead to the conclusion that the unit could not reliably perform its safety function at low ambient view more

One morning a saltwell pump was placed in operation. Operation of this equipment requires that the Standard Hydrogen Monitoring System (SHMS) cabinet be in operation. Later that morning, during the morning surveillance rounds, the Standard Hydrogen Monitoring System (SHMS) cabinet was found not to be in the operational mode.

On the previous day, the night shift saltwell operator assigned to run the saltwell pump had placed the SHMS monitor in operational mode; however, the saltwell system was not started at this time. Shift turnover was conducted and the condition of the SHMS was turned over to the appropriate saltwell operator and shift manager. During the day shift the day shift operator assigned to the complex received approval from the operations engineer to place the SHMS view more

During a facility walk-through, it was noted that a combustible gas (hydrogen) monitoring system installed in a furnace room was inoperable (the system had been unplugged). This system is used to detect and warn facility employees of an explosive or flammable environment. An explosive or flammable environment can only occur if there is a leak in the system, which would not be expected to occur during normal operations. When the system was reactivated, no leaks were indicated.

The incident had the following three causes:

A procedure describing administrative controls necessary to ensure safe operations in the area should have been developed and implemented prior to disabling the hydrogen monitoring system.
The hydrogen monitor was not hard-wired, which allowed it view more

An operator began preparations for a cleaning run, and was unaware that a maintenance task to calibrate a pressure transducer was scheduled to also take place that morning. The calibration required a break on a hydrogen line in order to install a Measuring and Test Equipment (M&TE) gage, which was used in the calibration. At the time the operator was informed of the calibration, the cleaning run procedure had been initiated but the actual cleaning had not yet begun. A discussion between his supervisor and the facility maintenance coordinator resulted in a decision to proceed with the maintenance task and suspend the cleaning run until afterwards.

The operator evacuated the hydrogen line and the hydrogen cylinder was valved out. The maintenance work package procedure had view more

As a prerequisite to a storage tank slurry pump run, a tank operator identified a Lower Flammability Limit (LFL) Analyzer surveillance reading to the control room that was out of limits low. The reading was a negative zero % LFL indication (-0 % LFL). The tank operator roundsheet limits are 0 to 10% LFL. The "null" value (value read on analyzer when air with 0% LFL is drawn through the analyzer) as directed by the LFL Analyzer loop calibration procedure is set between 0 and 4% LFL.

To alert personnel to the buildup of potentially dangerous levels of explosive gases in the tank, a Combustible Gas Detection System is used to monitor and analyze sample air drawn from the tank vapor space. This system consists of a sensing element, a 4-20 milliAmp direct current (mADC) view more

A bourdon tube ruptured in a pressure gage after 528 hours of operation in a liquid H2 system. The alarm sounded, the system was isolated and then vented.