CHECK OUT OUR MOST RELEVANT INCIDENT LISTINGS! 

Disclaimer: The Lessons Learned Database includes the incidents that were voluntarily submitted. The database is not a comprehensive source for all incidents that have occurred.

Personnel were focused on the AGES system test and results, not the compatibility of the test equipment. The manual valve was needed to successfully test the system, however the fact that this particular valve could not accommodate the full…

The hydrogen supplier installed a fire-resistant material board adjacent to the high-pressure hydrogen storage banks to prevent any potential jet flames from affecting adjacent high-pressure cylinders for several minutes. The 0.25 mm sandwich…

Because the bottle was located outside at the time of the event, and the hydrogen did not find a source of ignition while venting through the relief valve, nothing serious happened. The failed regulator was replaced and operations continued.…

The project team concluded that the jar contained a sufficient vapor pressure of isopropanol to ignite when it came into contact with the decomposing hydride. The lesson learned was that hydrides react rapidly in air and can lead to combustion of…

A hydrogen release of this type is a significant event. The event highlighted a number of procedural contributing factors that will influence the manner in which these fuel cell systems will be serviced in the future. A complicating factor in…

1.  Combustible gas detectors calibrated for hydrogen can falsely report hydrogen alarms due the presence of other gases the detector may pick up, such as carbon monoxide from engine exhaust or other sources. Since this event occurred, two…

Process changes have been implemented for development and review of safety basis documents that focus on a collaborative effort between the preparer and reviewers in order to provide a more in-depth review. This change is anticipated to provide…

A new best practice resulted resulted from this incident. It states that before any work is started, a third party should verify with a visual inspection that the actual equipment to be used matches the planned equipment list/protocol.

Several best practices resulted from this incident and will be implemented if similar circumstances present themselves in the future.

Close bay door.
Keep within proximity of bay.
Be aware of other bays operating with open…

Consider design review of all adapter fittings.

A tool is provided for removing the cylinder cap that cannot contact the valve.

1. The trailer involved in the incident used a frangible burst disk based upon the proprietary metal compound designated as Inconel #600. Random sampling of similar pressure relief devices from the same trailer showed that all of them failed at…

LESSONS LEARNED:

Compressed gas cylinder caps can be very difficult to open as rust often occurs in the threads.
There are wrenches specifically designed to remove compressed gas cylinder caps. The lab had such a wrench and it was…

Redundant safety systems prevented this event from becoming an incident. The 1%-hydrogen-concentration-level-triggered fan was backed up by a 2%-hydrogen-concentration alarm. The alarm is continuously monitored (24/7) by a remote Network…

Hydrogen safety training should be provided to local emergency responders.
Liquid hydrogen installations should be inspected by facility personnel on a frequent basis, consistent with NFPA 55, to verify proper operation and inspect for…

The possible outcomes from new maintenance scenarios can be predicted by using an accurate simulation. The proposed filter change-out maintenance was studied to identify conditions to which the catalyst might be exposed and a mock-up of the…

The following corrective actions have been taken:

The non-return valve was dismantled, cleaned, and tested. Following positive testing, the system was restarted and pressurized without any further malfunctioning.
The hydrogen…

The fitting was an SAE straight thread and was likely loosened by torque applied to the fueling hose. After the incident, these fittings had additional means applied to restrict loosening, a cover installed to deflect any leakage, and means taken…

Included inspection on monthly preventive maintenance plan and evaluated alternate materials for better cold-weather performance.

A gas detector was added in close proximity to the compressor shaft and a vibration switch is under consideration. Additional predictive measures are being considered to predict bearing failure. In addition, the manufacturer has been contacted…

Key:

  • = No Ignition
  • = Explosion
  • = Fire
Hydrogen Incident Summaries by Equipment and Primary Cause/Issue
Equipment / Cause Equipment Design or Selection Component Failure Operational Error Installation or Maintenance Inadequate Gas or Flame Detection Emergency Shutdown Response Other or Unknown
Hydrogen Gas Metal Cylinder or Regulator   3/31/2012
4/30/1995
2/6/2013
4/26/2010 12/31/1969     3/17/1999
11/1/2001
12/23/2003
Piping/Valves 4/4/2002
2/2/2008
5/11/1999
4/20/1987
11/4/1997
12/31/1969
8/19/1986
7/27/1991
12/19/2004
2/6/2008
10/3/2008
4/5/2006
5/1/2007
9/19/2007
10/31/1980
2/7/2009 1/24/1999
2/24/2006
6/8/1998
12/31/1969
2/7/2009

9/1/1992
10/31/1980

10/3/2008  
Tubing/Fittings/Hose   9/23/1999
8/2/2004
8/6/2008
9/19/2007
1/1/1982 9/30/2004
10/7/2005
  10/7/2005  
Compressor   10/5/2009
6/10/2007
8/21/2008
1/15/2019
    10/5/2009 8/21/2008  
Liquid Hydrogen Tank or Delivery Truck 4/27/1989 12/19/2004
1/19/2009
8/6/2004 12/31/1969   1/1/1974 12/17/2004
Pressure Relief Device 7/25/2013
5/4/2012
1/15/2002
1/08/2007
12/31/1969        
Instrument 1/15/2019 3/17/1999
12/31/1969
2/6/2013
    11/13/73    
Hydrogen Generation Equipment 7/27/1999     10/23/2001      
Vehicle or Lift Truck   7/21/2011         2/8/2011
12/9/2010
Fuel Dispenser   8/2/2004
5/1/2007
6/11/2007
9/19/2007
  2/24/2006
1/22/2009
     
Fuel Cell Stack            

5/3/2004
12/9/2010
2/8/2011

Hydrogen Cooled Generator       12/31/1969
2/7/2009
     
Other (floor drain, lab
anaerobic chamber,
heated glassware,
test chamber,
gaseous hydrogen
composite cylinder,
delivery truck)
  11/14/1994
7/21/2011
7/27/1999
6/28/2010
8/21/2008
12/31/1969
3/22/2018
    6/10/2019
  • = No Ignition
  • = Explosion
  • = Fire